Installing the new line turned out to be much harder than getting the old one out. First I had to buy the right components. Prefabricated lines come in a variety of lengths, and connect with special couplers to make up a given length. I needed to get the right lengths to make up a 13-foot brake line. I also knew I would need an adapter of some sort because the fitting that connected to the anti-lock brake controller was obviously not the same size as all the others. I wanted to do the job with the least amount of brake line and the fewest couplers because money was so tight.
I set off to my favorite auto parts store to get the pieces I needed. This is where I hit the first snag. They didn’t have all the sizes in stock, and they didn’t have the adapter I needed. I could make up the length from shorter pieces, but that raised the cost too much and added extra joints that I didn’t want. And it still left me without the adapter.
There are three auto parts stores fairly close to where I live. I prefer one over the others simply because it’s closer, the prices are better, and I get good service. But I needed my brake lines, so I headed out to check the other two. In the end, I had to get pieces from both of them. One had the lengths of line I needed, and the other had the adapter. Finally I had all the parts for the job.
Back home, I crawled under the truck and began bending the lines and snaking them along the frame. This went fairly easily, despite my not having a tubing bender. Modern steel brake line is much easier to work than its ancestors, and I was able to make the necessary bends without the tool. Leather gloves and strong hands did help, I might add.
I started at the back axle and worked forward. When I reached the front, I realized I had more line than I needed. I had not duplicated every tight little bend in the original factory line, so I reached the front of the truck faster. No problem. I just arranged the excess in a couple of artistic sweeps under the hood. The adapter worked as advertised, so everything was now connected.
I hoped to avoid dragging Folkcat out into the heat, so I tried to improvise some way of holding the brake pedal down and bleed the brakes without a helper. That didn’t work. I finally gave up and called her out to help.
With her in the cab pumping the pedal, I was able to start bleeding the brakes and finding the leaks. The bleeding went well enough, but the damn couplers wouldn’t stop leaking. I finally got the front one to seal tightly, but then the one in back wouldn’t stay tight. It seemed like I could get it to stop leaking, but then it would start up again on its own
It was slow and frustrating work, made worse by my fatigue. I didn’t realize how worn out I was until I lay down once more to slide under the truck. My neck muscles gave way and let my head crack down hard on the ground. I just lay there for a moment, unable and unwilling to move. I finally was able to move enough to resume work.
At that point, the stubborn coupler started leaking again and I started to lose it completely. Folkcat convinced to give up for the day. I listened to her. I cleaned up a bit, went inside, sat in front of the air conditioner, and slowly drank a bottle of cold water. It was the right thing to do. I had pushed too hard and gone too far.
Stay tuned for the next chapter…
-= Gryphon =-